Rotator control with a NodeMCU runs stable

My proof-of-concept works pretty stable - please check the status screen:


15-05-2016 16-15-33

It was running now for about 2.335.418s = 648h = 27d without any problem. The device answered nearly 1/2 million of position requests.

Due to a missing hardware control interface, the movement is very restricted.

The seleced virtual COMP port on my laptop works also stable - the connection surives Hibernation- and Sleep-Mode.